I am building a power supply for an ozone generator. It is a simple design, I will add feedback loops later. But for now I am trying to produce 4KV output(40W). But there is a problem with current. Micro-Cap simulations show that current is too much. Goes around 4 – 10 amps. If I put a multiplier to seconder it goes even higher like 20amps. What is the reason. How can I fix it?
Electronic – Flyback Mosfet Overcurrent Problem
high voltageozoneswitch-mode-power-supply
Related Solutions
The voltage spike created by the leakage inductance of your transformer is breaking down your MOSFET each time it switches off. You need to limit this voltage somehow; the usual technique is to put an R-C snubber across the source and drain of the MOSFET, sized so that the capacitor captures the energy of the spike before the voltage rises too high.
The values required depend very much on the characteristics of your specific transformer, so you'll have to do some experimentation to determine them.
One way to start is to find the value of the peak primary current in the transformer; the resistor should be sized so that this current, multiplied by the resistance, gives a peak voltage that's comfortably less than the rating of the MOSFET.
At the moment the MOSFET switches off, the drain voltage initially spikes high because of the leakage inductance of the transformer, but then it settles down to a voltage that's proportional to the secondary voltage (by the turns ratio of the transformer). The capacitor needs to be sized so that it charges to that voltage level in a time that's somewhat longer than the duration of the spike. This depends on both the inductance value and the resistor value. Be conservative at first (i.e., use an over-large value) and then fine-tune it (for better efficiency) once you have the circuit working.
It takes almost 2 mA just to charge and discharge the gate of your MOSFET. You're also wasting about 5 mA in R1, since it is grounded through pin 7 about half the time. Your voltage feedback divider is drawing about 1 mA from the high-voltage rail, which translates to more than 20 mA at the input.
There's a problem with using a 555 to drive a large MOSFET: The limited output current of the 555 means that the MOSFET can't switch quickly from full-off to full-on and back again. It spends a lot of time (relatively speaking) in a transition region, in which it dissipates a significant amount of your input power instead of delivering that power to the output. The MOSFET has a total gate charge of 63 nC, and the 555 has a maximum output current of about 200 mA, which means it takes a minimum of 63 nC / 200 mA = 315 ns to charge or discharge the gate. If you're using a CMOS 555, the output current is much less and the switching time is correspondingly longer.
If you add a gate driver chip between the 555 and the MOSFET (one that's capable of peak currents of 1-2A), you'll see a marked increase in overall efficiency. A real boost controller chip will often have such drivers built in.
If you're serious about developing switchmode power converters, you definitely need to get an oscilloscope so that you can see these effects for yourself.
That regulator design is also rather crappy for another reason. The power through a boost mode converter is regulated by varying the duty cycle of the switching element. In this circuit, the feedback is created by using a transistor to pull down on the control voltage node of the 555, which reduces the upper switching threshold. However, because of the way the 555 is constructed, this also reduces the lower switching threshold by a proportional amount. This means that the change in duty cycle as the ouptut voltage rises is much less than you might otherwise think. It has a bigger effect on the frequency of the output pulses, but this isn't relevant. Again, switching to a proper boost controller chip would solve this problem.
By the way, the "regulator" part of the circuit is NOT using the input voltage as its reference, it's using the forward voltage of Q1's B-E junction as its reference.
As Spehro points out, a 100 µH inductor at a switching frequency of 30 kHz — nominal on time = 16 µs — with a 9V source is going to reach a peak current of 1.44 A. This is really abusing the hell out of a 9V battery, not to mention the I2R losses in both the inductor and the MOSFET. This is also uncomfortably close to the saturation current of the inductor, which only exacerbates the losses.
Best Answer
Those 4 series diodes need 1MegOhm resistors across them, to ensure the reverse voltages are somewhat equalized. Or try 2.2 Megohm, or 4.7MegOhm.
Because of the high voltages, you should use discrete leaded 1/2 watt resistors.